The last straw?
Re: The last straw?
What was the problem with the smoke in the end?
did you get the bill for that too or was it a manufacturing fault with one of the parts?
how does it drive now?
i hope you decide to keep it, but i can understand why you are contemplating letting the beasty go.
take it for a nice drive in the country on a fine & sunny morning and see how it makes you feel. it might help with the decision.
All the best
Darren
did you get the bill for that too or was it a manufacturing fault with one of the parts?
how does it drive now?
i hope you decide to keep it, but i can understand why you are contemplating letting the beasty go.
take it for a nice drive in the country on a fine & sunny morning and see how it makes you feel. it might help with the decision.
All the best
Darren
Re: The last straw?
Dodgy new turbo, we reckon, another one has been fitted and seems to be ok
I haven't seen the bill yet, it will be posted to me in a day or two, I dare say they didn't want to see a grown man cry...
I haven't seen the bill yet, it will be posted to me in a day or two, I dare say they didn't want to see a grown man cry...
Re: The last straw?
Well, here's the latest...
I've had it back for about 7 weeks now and for the first six all was ok, but I'm sorry to say the nicotene patches have now failed and it's taken up it's old smoking habit, more than a Cuban prossie (so I've been told )
You can actually smell oil burning as you go along so it's going back on Thursday/Friday for another go with the mechanics...
Oh, by the way, for those interested...£3300, Included...
Bore out to +60 plus all new bits associated
new(recon) turbo
new radiator fashioned to fit (extra lower take off brazed in)
water pump
carb refurb
and a long list of all other tiddly bits required as you'd expect
I'm sure it's worth it
edited for a typo
I've had it back for about 7 weeks now and for the first six all was ok, but I'm sorry to say the nicotene patches have now failed and it's taken up it's old smoking habit, more than a Cuban prossie (so I've been told )
You can actually smell oil burning as you go along so it's going back on Thursday/Friday for another go with the mechanics...
Oh, by the way, for those interested...£3300, Included...
Bore out to +60 plus all new bits associated
new(recon) turbo
new radiator fashioned to fit (extra lower take off brazed in)
water pump
carb refurb
and a long list of all other tiddly bits required as you'd expect
I'm sure it's worth it
edited for a typo
Re: The last straw?
Ouch painful bill, is it coming out the exhaust or just smell of oil in car, could just be a weaping rocker cover gasket hopefully.......
Re: The last straw?
all out of the exhaust by the looks of it.
Blue on overrun, occasional black puffs at other times. You can hear the turbo spin up but it doesn't actually seem to propel you any faster.
Any way one good point is that when its taking me four hours to get home from work(via several hostelries);at this time of year its a bit warmer than back at the beginning of the year
Blue on overrun, occasional black puffs at other times. You can hear the turbo spin up but it doesn't actually seem to propel you any faster.
Any way one good point is that when its taking me four hours to get home from work(via several hostelries);at this time of year its a bit warmer than back at the beginning of the year
Re: The last straw?
valve stem oil seals? valve stems?
waste gate jammed open?
is it showing any boost on gauge?
Paul
waste gate jammed open?
is it showing any boost on gauge?
Paul
Re: The last straw?
apparently new valves, guides and correct turbo seals on refurb, but on inspection some of these seals had ridden up.
It was, according to the gauge on the dash, boosting to 0.2 first then onto 0.4 on real poke but didn't feel like it. Also, on full overun I do remember it sucking all the way down to -0.9 but now it only does -0.5.
I did wonder whether the issue I have with the boost modulator/solenoid (see earlier post) might have an effect but it didn't seem to. Any way I'm paying some else to get their hands dirty!!!!
Anyway returning to the origins of this post....
£7000, when fixed if anyone's interested....
It was, according to the gauge on the dash, boosting to 0.2 first then onto 0.4 on real poke but didn't feel like it. Also, on full overun I do remember it sucking all the way down to -0.9 but now it only does -0.5.
I did wonder whether the issue I have with the boost modulator/solenoid (see earlier post) might have an effect but it didn't seem to. Any way I'm paying some else to get their hands dirty!!!!
Anyway returning to the origins of this post....
£7000, when fixed if anyone's interested....
Re: The last straw?
New nicotene patch fitted in the form of some metal capped valve stem seals which apparently holds them in place better and some new valvey thing in the plenum chamber ( he began to lose me at this point!!) and some genral fiddling but the result is that at the moment it isn't smoking..just SMOKIN'
Scared m'self coming home!!
Scared m'self coming home!!
Re: The last straw?
it's about time you had some good news.
i hope this time it lasts many years before the engine needs any more attention.
All the best,
Darren
i hope this time it lasts many years before the engine needs any more attention.
All the best,
Darren
Re: The last straw?
The latest is that I removed the bolt from the u/s boost modulator and I nearly pooped myself!!!!
If you want to go faster thats the way to go.. unfortunately it blew some of the valve stem oil seals (the metal capped ones loctited in!!) so back it went for some new ones..
Bolt now back in situ, all calmed down but still very nippy and not smoking....and thats how I'm leaving it.
and with that, I think it's now time to close this thread..
I thoroughly appreciate all the support you guys have offered over the last few months..THANK YOU
Keeping/selling still don't know it's all tied in with house/work, but I intend to make to best of the remainder of the summer and make a few meets..hopefully see you out there....
If you want to go faster thats the way to go.. unfortunately it blew some of the valve stem oil seals (the metal capped ones loctited in!!) so back it went for some new ones..
Bolt now back in situ, all calmed down but still very nippy and not smoking....and thats how I'm leaving it.
and with that, I think it's now time to close this thread..
I thoroughly appreciate all the support you guys have offered over the last few months..THANK YOU
Keeping/selling still don't know it's all tied in with house/work, but I intend to make to best of the remainder of the summer and make a few meets..hopefully see you out there....